innes16v
Member
Registered: 22nd Jul 09
Location: Scotland
User status: Offline
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fitted a forge blanking plate today, took it a run drove boosted perfect, on my way home it stopped boosting, it runs fine, idles fine, no boost pipes leaking... anyone have any ideas? thanks
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Robin
Premium Member
Registered: 7th Jan 04
Location: Northants Drives: Clio 182 Cup
User status: Offline
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Recirc blank is not fitted properly IMO
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alan-g-w
Member
Registered: 9th Nov 07
Location: Glasgow
User status: Offline
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Fallen off if it's not boosting at all.
I had a similar thing and realised my actuator arm had come unhooked, do a couple of visual checks on the turbo itself and check everything looks right
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innes16v
Member
Registered: 22nd Jul 09
Location: Scotland
User status: Offline
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Theres only really one way it can be fitted... Fitted it... Took it a run, went great boosting a lot better, dump valve sounded great... Then was almost, home and it will hardly boost now but runs fine and ticks over fine, it will go to about 0.2 bar, tryed unplugging the senser or turbo to see if it was that, engine management came on so don't think it's that... Tryed maf senser, same again, then air flow meter same again so don't think it's that.... Checked all boost pipes, all fine. Checked vaccums seem to all be fine... Dumb valve seems to be open the hole time apart from when u rev it... Iam out of ideas, out it on computer... No faults
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Robin
Premium Member
Registered: 7th Jan 04
Location: Northants Drives: Clio 182 Cup
User status: Offline
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If that's the only thing which has changed it must be that.
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Robin
Premium Member
Registered: 7th Jan 04
Location: Northants Drives: Clio 182 Cup
User status: Offline
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Could be that it's not seated properly and is allowing the boost to leak past it.
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innes16v
Member
Registered: 22nd Jul 09
Location: Scotland
User status: Offline
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Sorted! Waste gate was stuck... No idea why... Lol
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